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TPS3895: TPS3895A output can't be released to high level

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Part Number: TPS3895

Hi

I use the TPS3895ADRYR as a power on reset signal.

The target voltage= (1+511k/110k)x 0.5= 2.82V. 

I know TPS3895A output is push-pull , so I depopulate the R746.

However, I can't see the reset (output) release to high level.

I check the figure 1. of datasheet. It seems that Enable need to be released before Sense. 

I measure my EN and Sense which is shown below (P1)

Enable  is not released before Sense. 

Does the timing of Enable and Sense on P1 cause that output can't be released???

  

P1


TPS2546: Unexpected auto-wakeup from a USB disk

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Part Number: TPS2546

Hi,

Our customer encounter an unexpected auto wake-up issue (S3-->S0) shortly after their laptop has a S0-->S3 transition.  Some details as below,

  • Currently the issue is duplicable with 2 specific models of USB3.0 disk
  • The issue is not duplicable if ILIM_SEL is always low
  • When ILIM_SEL is high, the failed rate is pretty high.
  • S0 mode setting: CTL1/CTL2/CTL3 is "111"
  • S3 mode setting: CTL1/CTL2/CTL3 is "011"

Related waveforms as below.  Please share your in puts why it would wake up unexpectedly.

Normal S0-->S3  (CH1_CTL1 / CH2_VBUS / CH3_DM_IN / CH4_DP_IN)

Normal S3-->S0  (CH1_CTL1 / CH2_VBUS / CH3_DM_IN / CH4_DP_IN)

Abnormal wake-up (S3-->S0) happening immediately after S0-->S3 (CH1_CTL1 / CH2_VBUS / CH3_DM_IN / CH4_DP_IN)

Zoom-in of abnormal auto wake-up (CH1_CTL1 / CH2_VBUS / CH3_DM_IN / CH4_DP_IN)

Zoom-in of abnormal auto wake-up (CH1_CTL1 / CH2_VBUS / CH3_DM_IN / CH4_DP_IN)

THanks

Antony

TPSM84624: TPSM84624

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Part Number: TPSM84624

Hi there,

Last paragraph on Page 15 of the TPSM84624 datasheet says that "If using a combination of ceramic and polymer type of output capacitance, only a single polymer capacitor can be used.".

For me, it doesn’t sound too practical in real applications, since output capacitors in almost all applications are comprised of ceramic and Polymer or Tantulum or Os-CON or both. What do you think?

Thanks & BR,

Ghasem

TPS54060A: Bad regulation with some units

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Part Number: TPS54060A

Hi!

We use the TPS54060A to generate +-17V from +24V (18..30V). As reference, we used the schematics of the evaluation board TPS54060EVM-590. At about 80% of all devices, the output voltage is stable. I mean if I varry the +24V to +19V, the output does not vary much, and for example only goes down 0.1V from 16.8V to 16.7V. The "good" devices also show not much impact when the current is increased from for example 80mA to 100mA. In contrast, the remaining 20% are very sensitive to the input voltage and also to the current drawn. Some exemplars show only +16.4V at +24V and less than +16V at +19V, so it varies with the input voltage. Therefore the negative voltage goes even more negative to for example -18V and less, I assume the sum stays approx. 34V. For regulation, we first used two resistors at input VSENSE (see the schematics below).

A hint by someone of this forum was to add a third resistor to GND (R99), to balance it out. But also this third resistor did not really help.

We then increased the resistor to the positive side (R40) to bring the voltage up. For example, we incresed the resistor so that a device that shows only +16.4V outputs nearly +17V. The drawback is that the negative voltage goes more negative, but this we think is no problem for us.

Unfortunately, this does not really help, as the devices showing this problem are also very sensitive to the current drawn. If we increase from for example 80mA to 100mA, some examples show a voltage drop of appprox. 0.5V.

Has someone an idea? - Can it be a capacitor that causes this? Or the inductor?

Thanks!

BQ25710: Input current limit during REGN drop mode

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Part Number: BQ25710

According to my evaluation, the actual input current limit is lower than the setting value if REGN in during the drop mode.

 - Setting value = 3.25A

 - Actual value = 2.8A

The condition is VBUS=5V, CELL_BATPRESZ=2-cells, MinSystemVoltage=6.144V(Default and without BatteryPack.

If VBUS or MinSystemVoltage >7V, the actual input current limit is set to the expected value.

The input current limit is affected by REGN voltage because the the internal ADC doesn't use the ratio metric.

Is my thought correct?

If YES, can you share the data of the actual input current limit during REGN drop mode when the setting value is 3250mA?

Thanks

Tamio

 

BQ76930: What happens to bq7693003 device if one of the pins had been open from PCB ?

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Part Number: BQ76930

Dear all

        What happens to bq7693003 device if one of the pins had been open from PCB ? 

        As below is our sugessing , please help me to check " Potential Failure Phenomenon ", and redress them, Thanks a lot.

BQ34Z100-G1: Learning Cycle Failure to Converge

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Part Number: BQ34Z100-G1

I'm trying to understand why the learning cycle failed for the BQ34Z100. Log attached

I've followed the instructions here (page 52) and here, and believe I've followed the appropriate steps and waited enough time between charge/discharge during the test. I'm using a 4S LiPo battery configuration (each cell operates between 3V (terminate) and 4.4V (full charge), with a 4500mAh capacity.  I had previously used the Chemistry GPC tool to get a chemistry ID match (1601 was the best match with 0.84 Max DOD error)

Differences observed from expected behavior:

1. The FC bit was set prior to the charging cycle finishing.  I continued charging for about ~15 minutes more to wait for the charge current to fall below 100mV.

2. After charging was complete, the documentation says to wait ~2 hours for the battery to relax, at which point the RUP_DIS = 0, VOK = 0, OCVTAKEN = 1, and Learned status changes from 04 to 05.  This all happened as expected, but only about 20 minutes after the charge stopped.

3. Even though it appeared ready to discharge, I waited for over 2 hours per the documentation before beginning discharge

4. I discharged at 900mA (C/5).  At the very end of the discharge, the fuel gauge was indicating that the battery should be completely discharged (SOC = 0, remaining capacity = 0, etc.) prior to it actually getting there.  It took close to 5.5 hours to discharge completely when 5 hours was expected (the actual battery capacity appears to be higher than the nominal capacity listed in the datasheet).  Shortly after indicating that the battery should be discharged, the RUP_DIS bit became set.  About 10-15 minutes later the battery pack fell below its termination voltage (12V) and I stopped the discharge.  The battery relaxed, but the learned status was still stuck at 04.

According to the documentation, the RUP_DIS bit becoming set during discharge can indicate that the chemistry selection is not appropiate.  I used my log from the failed learning cycle with the GPC tool, and the chemistry I used (1601) comes back in the list with max DOD error = 1.31 (there are others chemistries with lower errors this time around, but it seems like this would still be an acceptable chemistry).

Any thoughts on what I need to change to get the learning cycle to complete?  I'm in the process of completing another charge/discharge cycle without changing anything in hopes that it will converge after another cycle.

Any help or ideas would be much appreciated.

(Please visit the site to view this file)

BQ78350-R1: What happens to BQ78350-R1 device if one of the pins had been open from PCB ?

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Part Number: BQ78350-R1

Dear all

        What happens to BQ78350-R1 device if one of the pins had been open from PCB ? 

        As below is our sugessing , please help me to check " Potential Failure Phenomenon ", and redress them, Thanks a lot.


TPS7A16: What happens to TPS7A1650 device if one of the pins had been open from PCB ?

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Part Number: TPS7A16

Dear all

        What happens to TPS7A1650  device if one of the pins had been open from PCB ? 

        As below is our sugessing , please help me to check " Potential Failure Phenomenon ", and redress them, Thanks a lot.

TPS92641: Design tool for TPS92641

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Part Number: TPS92641

We want to design Vin=12V, Vout=3.7V Iout=25A and Vin=12V, Vout=8V Iout=10A use by TPS92641 LED driver.

we saw that there are some formula to defind the value of Resistance and Capacitance,but maybe it is complex

But WEBENCH tool can not support TPS92641,so did have special design tool for LED driver like TPS92641

Thanks

LM5008: What happens to LM5008 device if one of the pins had been open from PCB ?

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Part Number: LM5008

Dear all

        What happens to LM5008  device if one of the pins had been open from PCB ? 

        As below is our sugessing , please help me to check " Potential Failure Phenomenon ", and redress them, Thanks a lot.

BQ76200: What happens to BQ76200 device if one of the pins had been open from PCB ?

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Part Number: BQ76200

Dear all

        What happens to BQ76200  device if one of the pins had been open from PCB ? 

        As below is our sugessing , please help me to check " Potential Failure Phenomenon ", and redress them, Thanks a lot.

UCC28063: UCC28063 about θjc

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Part Number: UCC28063

Dear,

currently our client want do derating ,so we need UCC28063 θjc value.

Specification

Vcc/Vin
(Peak)

PD

Temp
(℃ )

(V)

(W)

θjc

Tj

21

0.890

 

125

if any suggestion, Please advise me.

Thanks,

Best regards,

Lawrence.

UCC256302: Different burst mode point at different input voltages

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Part Number: UCC256302

Hi Tiers

My project is 195~255Vac input and 130W output, I use the UCC256302 without PFC,

When the input voltage range is 195Vac~230Vac, the brust mode is 0.1*Load(about 13W),

When the input voltage range is 230Vac~2550Vac, the brust is 0.3*Load(about 39W),

Is this normal?  Can we get this parameter closer?

BTW,  Is there a good way to solve the noise when the light load?

thx

BQ34Z100-G1: BQ34z100-G1 CC Gain and CC Delta decimal value conversion to Hex

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Part Number: BQ34Z100-G1

Can somebody provide the formula to convert the CC Gain and CC Delta decimal value to Hex Value.


TPS54232: Efficiency Curve of 20V to 5V

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Part Number: TPS54232

Hi there,

1. I'm considering to suggest TPS54232 to customer for Home appliance solution. I need efficiency curve (or just rough number of efficiency) of 20Vin to 5Vout. I only can find the efficiency curve for 3.3V output in the datasheet.

2. I also need efficiency information when 20Vin to 12Vout. I guess it would have very low efficiency as it is non-synchronous type. So I'm considering synch-type converter, but most of step-down converter data sheets provide efficiency curve only for 5Vout, 3.3Vout, and 1.8Vout. Is there any way to figure out the efficiency for higher output voltage?

Thank you in advance for your help!

BQ24166: Switcher output bad if USB voltage is higher than 5V

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Part Number: BQ24166

Hello,

I am having some strange issue with BQ24166 in that if the USB input voltage is any higher than 5V (this threshold varies slightly board to board but it is right around 5V) the output becomes very unstable.  Here is what i mean:

Switcher Voltage output (VBAT from circuit below) when USB < 5V:

Switcher Voltage output (VBAT from circuit below) when USB > 5V:

Both scope plots above you are looking at a time when i power on the board at the trigger point, you can see the < 5V image there is basically no droop on the output and it just stays pretty consistent, if i zoom in i can see a miniscule droop during the inrush current.  For the USB > 5V you can see the output is already lower and highly unstable then when i power on the board the inrush current pulls the voltage low enough to cause the board to brown out and turn off allowing the voltage to rise again.

I am not sure what the issue is, it is fine at 5V and lower but the problem is i can't control the voltage supplied by a given USB port and often times they are slightly above 5V, so when that happens the board just won't run without a battery.

Here is my circuit:

Any ideas what i have done wrong or what the problem could be?  Note i have tried swapping C99 to a 47uF capacitor to no avail.

Thanks,

Jarrod

LM5116: LM5116 load issue

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Part Number: LM5116

Hi Tiers:
I use the LM5116 in my DC/DC project

input:50V

ouput:12V1A

when the load is CC<0.6A, all waveforms are normal.

but when the load is CC>0.6A, the waveform is not normal, just as below:

C2 is low-side MOS gate driver

C3 is the Inductive current waveform

All the SCH parameters are from the Webench.

Could you give me some suggestions to deal with this issue?  thx

TPS54540-Q1EVM-593: Excel BOM

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Part Number: TPS54540-Q1EVM-593

Hi Team,

Can you please share the excel version of the TPS54540-Q1EVM-593 BOM? My customer has the PDF from the user's guide but the excel would be helpful to price it out.

Thanks,

Antonio

LM5121: UVLO, the equation to determine the values of RUV1 and RUV2

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Part Number: LM5121

Hi,

In LM5121, I don't understand how does the equation1,2 and 3 come out?  

Besides, I also want to know is the output overvoltage protection realized. Thank you so much.

Best Regards,

Wenxiu

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